I cant paste it in C code
It is working, thank you!
Type: Posts; User: mk00
I cant paste it in C code
It is working, thank you!
It is till too long
(0 , 0 , 0 , 0 , 0 , 0, 0 , 0 , 0 , 0 , 0 , 172.981068 , 306.17 , 315.544674 , 344.282368 , 373.545116 , 392.323716 , 427.690896 , 458.933405 , 485.601278 , 530.027746 ,...
Another problem has arisen, I will not create a new topic. I am setting up a new lathe. I set up both axes, they move good in Kmotion step response, from C code and manually in KMotionCNC. But when i...
Hi, Tom
Version 4.35f
I want to use long constant 2D array string with dependence of RPM on PWM frequency of my spindle. When I paste it in C editor window Kmotion stops working. When I try to...
I tried a different version of the firmware file and it worked. May be my file is corrupted.
Hi Tom
I tried to flash user memory, but the KMotion stopped responding. When I rebooted the computer and the Kflop, the Kflop did not boot. It flashes diodes several times and they go out.
I...
It works, thank you!
Hi, Tom
Today I turned on my machine and the KMotion did not see the klfop, it is not presented in the system. When powering, the Kflop flashes with diodes, but instead of constantly burning, the...
After the weekend it worked. Nothing has changed. I think that the problem is in my PC. In any case, thanks for the reply.
Hi, Tom
Everything worked well for a long time, but this morning KMotionCNC could not open the configuration file. I decided that I had some problems with the disc, checked everything, found...
At first I thought that when moving around the axes with the Move command, the Z geo correction is lost, but this is not the case - Z changes accordingly when moving. The assumption that the length...
Like I solved the problem. When measuring the length of the tool, sometimes the geo offset turned out to be different, although the measurement always occurs at one point. I was not able to find out...
I measure tool length after each change. The spindle moves down at MoveAtVel command to the measurement device until the contact closes.
I would like to get the geo offset directly as OriginOffset...
Addition - MDI does not work only in exec/wait and exec/wait/sync modes, it works in the "execute prog" mode, but such use is not possible.
Since we are on different sides of the planet, just in case, I will clarify.
When using Move commands, correction does not occur and the coordinate is lost. If I could get the geo correction Z...
I tried to move spindle in the same position before tool change with MDI command, it works from KMotion, but dont work from KMotionCNC, nothing happening on MDI command!
Hi, Tom
I decided to use the geo correction to improve the flatness and encountered a problem in measuring the length when changing the tool. When changing a tool, I use the MoveAtVel function in...
No, both CAM and KmotionCNC in millimeters. If I will increase radius manually by 0.001 all will work
Hi, Tom
Here is example program. May be it is possible to modify postprocessor, but i dont know how. I`we read that LinuxCNC have option for adjusting arc endpoint tolerance.
Hi,
KmotionCNC sometimes tells "arc radius too small" on my programs, although in Mach3 all is good. At this moment I solved this by increasing radius by few microns manually. It there a way to...
With 4.33n all is good, thank you Tom.
In the console is displayed 4.33m. May be it is wrong firmware file? Or revision of the board is important? I`ll run program tomorrow.
I run your code without modification, yes it is short capture. Here is correct capture - like your first graph.
Here the result. Motion abrupt at 6200 steps (beginning of deceleration?). Also I noticed that with 4.33m problem occurs with any movement, not only with small movements.
No, the behavior remains the same. Version 4.33m. This occurs during deceleration. On your graph axis in not marked, is this speed or position. This is my full init for this axis:
...
Hi, Tom
This occurs during deceleration with small movements, like 800 steps with 10000 velosity and 10^5 acceleration, 10^6 jerk. Now I set 5*10^4 acceleration and 10^8 jerk - looks ok.
with large amount of jerk, like 10^8, works ok
but anyway that operates in 4.32 not working in 4.33l
no, problem with small movements
addition: with Jog and Move comands all is good, MoveRelAtVel is bad.
I have issue with 4.33l firmware. One of my steppers twitches on stop and lost steps, on accleration all looks good. All parameters and initialization are the same as with 4.32 firmware, but with...