Hi!
OKUMA LB12, OSP500L, 1990 YOB.
I changed X axis motor (old was too noisy) and had got such error (100-3 alarm-a dif over) or 102-3 alarm-a apa velocity (see photo).
How can I adjust encoder? Have anybody doc about change motor procedure?
I understand that diff of my new encoder and stored in bubble memory is very big. And first error 100-3 tell me about it. But second error 100-2 tell me that velocity to correct diff is too much.