Let's look at this from an operator's standpoint and the burden it creates...
In an environment where one operator has to run several machines this creates an overload of unnecessary added stress...
Type: Posts; User: nitemare
Let's look at this from an operator's standpoint and the burden it creates...
In an environment where one operator has to run several machines this creates an overload of unnecessary added stress...
steve,
on the way up from the top of the part: G0Z3.M1019 would be correct? then the line for the tool change
the control is an MSG 805...machine is about 10 years old. i spoke with a tech today and he said that an m1005 will ignore the signal that the tool has stopped and ignore the spindle orientation and...
is there any way to reduce the wait for the spindle to stop for a tool change? we have a mori gv503 3 axis mill. it takes 5 seconds for the spindle to stop from 12000 rpm. if we program an m5 before...
i run G97 when ramping into position...
G97S2200M3
G0X2.1Z.1T0101M8
G96S800
i use G97 for drilling, threading, tapping, etc...all fixed rpms
i use G96 almost religously for all other...
I believe the BAUD RATE would be 4800, stop bits 7, parity even, can't remember what the other bit is but it's 2, and ours run no handshake...(XON/XOFF etc...)Had to reset this a few weeks ago...
Running a Quickload Servo 80 LNS Bar feeder on a 2008 Okuma Captain L370. Does anyone have a sample program for the bar feed cycle. I'm new to this servo style machine as are existing bar feeder is...
HIGBEE! It sort of works...i still get a bit of a sharp edge where the first full thread is at the major Ø...here's what i have:
N7T0303(THREAD O.D.)
(3.5 - 5 BUTTRESS)
(KENNA NTB4RB KC5025...
not quite sure what you mean here. pardon the stupidity, but i'm a bit slow on the uptake. i have a 3.5 inch, 5 threads per inch o.d. thread. so, my pitch is .200", and the thread is 45°, 7°; the 45°...
just went through a similar scenario. threading 1.875"-12 i.d. in 304SS, 2.00" deep in a blind hole. ended up with a vardex 3 sided 12 pitch vtx or vkx grade - both worked well. used 2 degree modifed...
i contacted our local service tech on this exact issue. osp700L and ospu10L. they gave me a parameter to change and VIOLA! worked. can't remember what or where the parameter was...been some years...
i am currently machining a modified O.D. 3.5"-5 buttress in DOM tubing. by modified, i mean that the customer has changed the major Ø and minor Ø to accomodate their customers mating part. the mating...
Now you took all the fun out it Bad Dog... LOL!
No c-axis...:(
yeah...m19 works fine by itself but nothing i try will lock it at a specific angle. guess i'll have to do with out.... :confused:
is there a way to orient the chuck at a certain angle. i know on okuma i can give it an m19 c### , c being the angle. tried this on puma 250, but nothing works.
Also, is it a safety feature that...
ok. i made a post about offset shifting - i was confused. allow me to retort:
i need to make some washer type pieces. dims: 3.00" o.d. x .31 thick, then drilling a .766" dia. hole.
i want to...
ok. i have to make several washer type samples. they will be 3.00" dia. x .3125" thick. i would like to make 5 pcs before bar pull. someone tells me that i can use a G52. is this possible? i think it...
that will work awesome for me. every few days im doing a new program and about 70-80% of them are pipe threads. thanks a ton. my life is getting easier! :cheers:
Thanks a ton. That helped tremendously. Makes more sense to me now.
i need to run 5 snap ring pieces per cycle - using bar pull op - is there a simple way to repeat the program? i will face, drill, o.d. & i.d. groove for edge break, and then part off all five. The...
Thanks. I'll give it a shot and let ya know.
Any help on this one? having diffuculty with the G76 cycle. Are there any "simple" ways to calculate for X, P, R, etc????? I'm new to this whole tapered thread thing and evidently, so is everyone...