I am having problems getting my superfly cutter working with my 770 machine and some low carbon steel, and was hoping someone may have some insight.
I'm trying to face my stock before I begin work on what will eventually be a prototype; the first time I tried to face my steel, my settings were as follows, taken from the g-wizard program;
Spindle Speed: 479 RPM
Cutting Feedrate: 120 mm/min // 4.72 in/min
Depth of Cut: 0.75mm // 0.0295 in
The carbide insert bit down, and refused to cut any further before I hit the e-stop.
Second time around, I used specs from the Tormach Fly Cutting demonstration video, but I was more conservative with my depth of cut;
Spindle Speed: 1000 RPM
Cutting Feedrate: 254 mm/min // 10 in/min
Depth of Cut: 0.25mm // 0.0098 in
The insert bit down again, but moved no further than the first attempt. Can anyone give any suggestions as to why this might happen, and what I should be doing to fix it? Many thanks in advance.